Decided to put the piston in my family 4 seater and try it out, will order another for the race car next week. The crank didn't get done in time for me to put the race motor back together this weekend.
Started at about 1:30pm yesterday, tore the top end off, and put the 102.5 piston in. I had a cylinder machined earlier this week for it. I put my ported head with +1 valves on it and a hot cams stage 3 cam I had sitting on the shelf. It has a stock clutch sheave and strock spring with hunterworks overdrive weights. Muzzy pipes and a mikuni 45 rounded it out. Had it all back together by 10pm.
Set the jetting to 12.5 to 1 at WOT with the air fuel meter and did some runs.
It was hitting a rev limiter at 62mph. Checked and it had a Dragonfire procomm CDI. Drove it over to Scott from XMFs house and stole his Dynatek CDI (he wont be needing it for a while). Now it pulls to the rev limit at 69mph. Not to shabby.